Right guys and girls I was at MRC yesterday trying to get a few more psi out of my car, so after sorting the boost leak and a change of oil for the rear diff we set out to see what we get, two weeks prior to this I was achieving 25psi and 21 and red line with maf reading of 405 on standard 2" no cats downpipes so I changed to rs4 downpipes to see what we can get. We headed off and was only achieving 22psi and 18 at red line she has dropped

come back another pressure test change of n75 valve mind you every sensor on this car is brand new the engine was built from crank up and engine is only covered 2k with 1k being with the n75 unplugged, still no change so we was going to put it down to hot sides problem when Doug goes check the dv's I said there brand new apr r1 £100 each so we decided to check them anyway and there was the problem they were fooked

bits of the internals of the dv was flying around lucky none went into my turbo well put the 710's on and away we go

very happy with end result.
that shows sometimes you cant beat standard parts ollyW took some pictures hopefully he can add them to the post for you lot to see
cheers