First off, hats of to Doug and his team - great event and all the staff and Doug were more than happy to help with the cars where possible.
Mine went on the Dyno ... first run .... 339PS !
not good .... vacuum leak
Now, when I first picked up the car from its previous owner, it felt quick ... I mean proper quick ! much faster than the RS 4 Cab.
THEN, within a few days I took it to Paramount Performance in Slough, to fit my Non Res Non Valved Milltek.
Ever since that fitting, it never felt the same.
I even said to iR8V8 (RS6_Dave) at a meet a few months back that I suspected it had a vaccum leak as it had lost its 'kick'
but, then for the National RS 4 Meeting, in drags against TimsterRS4 and scaghead, the bananananana held its own....nothing in it, neck and neck !!!!
so, must just be me...
but, then the dyno reading does not lie !!
So, the MRC boys head to the most obvious leak, in the air box i think ... 2 second fix, next run .... 370PS
ok, now we're getting somewhere ...
next run 350PS ! hhmmmmmm .... another leak? Doug can hear a hissing from the rear
Exhaust valves
Turns out, upon fitting my Non Valved Milltek, the cowboys at Paramount Performance decided against bunging up the valves ... thus allowing loss of vacuum
So, bung up the valves .....
386.7PS
BOSH !
So, two lessons learnt
1. trust your instinct ... if it doesnt feel right, it prob isnt
2. dont ever use Paramount Performance as they evidently dont have a fecking clue
Finally, huge thanks to Doug and MRC for showing their expertise and having the good grace to sort the leaks on the spot
I will be a returning customer .... which is more than I can say for you know who in Slough

oh, and all for the pricely sum of £45, from 339PS to 386.7PS
